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Article

Prediction and Control of the Nitrogen Oxides Emission for Environmental Protection Goal Based on Data-Driven Model in the SCR de-NOx System

1
Xi’an Thermal Power Research Institute Co., Ltd., Xi’an 710032, China
2
Nanjing NR Electric Co., Ltd., Nanjing 211102, China
3
Hebei Technology Innovation Center of Simulation & Optimized Control for Power Generation, North China Electric Power University, Baoding 071066, China
4
School of Electric Power, Civil Engineering and Architecture, Shanxi University, Taiyuan 030006, China
*
Author to whom correspondence should be addressed.
Sustainability 2022, 14(19), 12534; https://doi.org/10.3390/su141912534
Submission received: 13 August 2022 / Revised: 15 September 2022 / Accepted: 27 September 2022 / Published: 1 October 2022
(This article belongs to the Special Issue Multiscale Nitrogen Emission and Its Impacts)

Abstract

:
In order to reduce the nitrogen oxides (NOx) emission of flue gas, a selective catalytic reduction (SCR) system must be installed. In general, the lag of the inlet NOx analyzer, the action of the NH3 injection valve and the feedforward signal are seriously delayed. Therefore, it is necessary to consider the measurement lag of inlet NOx on the NH3 injection flowrate control system. In this paper, the data-driven model of inlet NOx is proposed to improve control system, so as to avoid excessive or insufficient NH3 injection. First, the measurement lag time of inlet NOx is estimated by the blowback signal of a CEMS and the change process of the inlet O2 content. Then, an exponential model is used to predict the inlet NOx in advance, and recursive LSSVM is proposed to revise the output of the exponential model. Finally, the output of the final model is used as the feedforward signal for improved feedforward (IF) control. Based on IF control and PID control, the IF-PID control strategy for NH3 injection is proposed. The results show that the outlet NOx are close to the set value and meet the national environmental regulation. Furthermore, the average value of the NH3 injection flowrate remains unchanged. It shows that a better control effect and environmental sustainability are achieved without increasing the cost of NH3 injection.

1. Introduction

Coal-fired power generation is currently the main form of power generation in thermal power plants, and the coal burning in boilers produces large amounts of nitrogen oxides (NOx), which are absorbed by rain and snow as they fall and are generated in the atmospheric system, resulting in acid rain that can cause building corrosion and crop death, thus affecting the sustainability of natural resources. NOx also reacts photochemically with other pollutants in the ultraviolet light, creating secondary pollutants known as photochemical smog pollution. If it encounters fine particles in the air, it will form PM2.5, thus endangering the survival of animals and agricultural crops, thus destroying the balance of the ecosystem and causing significant pollution to the environment. So, NOx emissions from thermal power plants have been under strict supervision. In China, it has been required that NOx emissions be reduced to below 50 mg/m3. On the one hand, the valve life is easily affected by the frequent action of the NH3 injection valve. On the other hand, if the NH3 injection is less frequent, it is easy to cause the outlet NOx to exceed the national environmental protection standard and allow the NH3 to escape, causing secondary environmental pollution [1]. Flue gas denitrification technology is used to denitrify the exhaust gas from the coal combustion. A selective catalyst reduction (SCR) system is the current method used by the majority of thermal power units. The common reducers for a SCR system are liquid ammonia, urea and ammonia water. The use of ammonia water as a reducing agent can not only avoid the use of liquid ammonia with high safety risks, but also avoid the use of urea with high operating costs. Due to the large inertia of the SCR system and the response lag of the NOx analyzer, the control effect of the traditional proportion integration differentiation (PID) control method is poor. So, it is difficult to put the control system into an automatic mode. In addition, the response lag of the NOx analyzer is up to 1 min, so the SCR system is different from the conventional large inertia control object and has a negative impact on the control effect. So, the existing feedforward control strategy received attention.
The direct reason which affects the fluctuation of the outlet NOx concentration is the fluctuation of the inlet NOx concentration, so the control effect of the outlet NOx concentration will be affected directly when the inlet NOx concentration has a large fluctuation. In order to improve the control effect of NH3 injection, it is necessary to consider the response lag of the inlet NOx analyzer. Although many studies have solved the large inertia of the SCR system by improving the control method, the source of lag is less studied [2,3]. The lag time is mainly caused by the NOx analyzer in a continuous emission monitoring system (CEMS). The response lag of the inlet NOx analyzer leads to the NH3 injection valve action slowly. So, the SCR control system cannot eliminate the lag which undoubtedly increases the difficulty of the NH3 injection flowrate control and causes the outlet NOx fluctuation [4,5]. Therefore, by studying the data-driven model of the inlet NOx concentration, the effect of lag on the SCR system can be compensated to some extent.
Some scholars proposed data-driven techniques to build prediction models based on the field data. Shakil et al. [6] established the dynamic neural network (NN) model of the inlet NOx concentration and inlet O2 content in the SCR system, and principal component analysis (PCA) is then used to reduce the dimensionality of the input matrix, estimate the lag time by genetic algorithm (GA) algorithm, and finally validate the NN model by field data. Hsieh et al. [7] proposed the data-driven model of the NOx concentration based on Kalman filtering and the data fusion technique to overcome the lag time of the SCR system, but the method only used a lag time within 200 s. Peng et al. [8] proposed PCA and SVR models to make more accurate and rapid forecasting of the inlet NOx concentration, respectively. Lv et al. [9] used a model combining an internal LSSVM model with an external linear PLS to predict the outlet NOx concentrations. Li et al. [10] proposed a modelling approach which combines the moving window partial least squares (MWPLS) and partially weighted regression to predict the outlet NOx. However, the above method can only predict the inlet NOx concentration at the current moment. Ahmed et al. [11] used a real-time update strategy based on LSSVM to predict the NOx, and it enhanced the long-term prediction accuracy. However, the model has some deviation when the boiler is under variable operation conditions. Yang et al. [12] proposed a real-time dynamic prediction model of the inlet NOx concentration based on LSSVM and considered delay time and prediction error. Xie et al. [13] proposed a sequence-to-sequence dynamic prediction model to predict the future outlet NOx concentrations. In addition, some scholars analyzed the effect of the inlet NOx concentration measurement lag on the control effect by predicting the inlet NOx concentration in advance. Matsumura et al. [14] eliminated the effect of lag time to some extent by predicting the inlet NOx concentration in advance with LSSVM, which improved the control accuracy and reduced the operation cost. Kříž et al. [15] estimated the time delay by using the Lyapunov exponent and embedding dimension. Kang et al. [16] proposed a bidirectional long- and short-term memory (LSTM) neural network and estimated the lag time of SCR systems by dynamic joint mutual information (MI). Song et al. [17] used an improved MI feature selection algorithm to filter out the input variables of the inlet NOx concentration model. The input variables are then fed together into the LSTM neural network to build the model. Liu et al. [18] selected 22 key variables of the power plant and built the multiple linear regression (LR) model with three hidden layers. Wu et al. [19] proposed the least absolute shrinkage and selection operator to select input variables and used long short-term memory to establish the model. Yuan et al. [20] combined PCA and SGEM method to build an inlet NOx concentration model. The MI method was used to select the input variables of the inlet NOx concentration model. Li et al. [21] built the mechanism models of the SO2, inlet NOx concentration and O2 content, respectively. Then, the improved RBF neural network was then adopted to compensate the prediction error.
Table 1 shows the advantages and disadvantages of different data-driven techniques from different aspects in the literature [6,7,8,9,10,11,12,13,14,15,16,17,18,19,20,21]. The shortcomings of the existing literature are mainly the following two aspects: First, there is a lack of clarity in the analysis of the CEMS measurement lag. Second, there is a lack of quantitative conclusions.
Therefore, in order to improve the control effect of the NH3 injection flowrate, this paper proposes to improve the existing feedforward control strategy. Firstly, quantitative analysis is adopted to estimate the lag time, and it improves feedforward (IF) control by establishing an improved exponential prediction model for the inlet NOx concentration and using the output of this model as a feedforward signal. Secondly, in order to further improve the control accuracy of the PID control, an IF-PID control is proposed. Finally, the PID and IF-PID control are compared.

2. The Lag Time of the Inlet NOx Concentration

In this paper, a quantitative estimation of the lag time of the inlet NOx concentration is required before building a data-driven model. Firstly, the reasons for the lag time are analyzed in this section; then, the analysis method for estimating the lag time is proposed.

2.1. The Reason for the Lag Time

A CEMS comprises a gaseous pollutant monitoring subsystem, a data acquisition and communication subsystem, a flue gas parameter monitoring subsystem and a particulate matter monitoring subsystem. Here, we analyze the gaseous pollutant monitoring subsystem involving NOx and SO2 monitoring, whereby the CEMS extracts flue gas directly from the flue through the long pipe. Flue gas is directed to the pre-treatment system for dust removal, dehumidification and corrosive gas treatment, and finally reaches the flue gas analyzer. Measurement data from the flue gas analyzer are transmitted to the industrial control computer for processing, thus realizing the real-time monitoring of NOx and SO2.
The schematic diagram of SCR de-NOx system is shown in Figure 1. The flue gas channel at the exit of the economizer is divided into two paths, each path of flue gas corresponds to an SCR reactor, and the flue gas enters the catalyst layer after passing through the flow equalizer. At the same time, before the flue gas enters the catalyst layer, the mixed gas of NH3 and air enters the ammonia injection grid, and then reaches the SCR reactor, where it reacts with NOx in the flue gas under the action of the reaction temperature (280~400 °C) and the activity of the catalyst. The flue gas after the reaction is discharged into the chimney through equipment such as an air preheater, electrostatic precipitator and induced-draft fan.
Because the measurement of the NOx concentration requires a long pipe to reach the NOx analyzer and the analysis of NOx also takes some time, this is the reason why the CEMS measurements have a long lag time.

2.2. The Analysis of Lag Time

Because the blowback signal of the CEMS is usually accessed in the distributed control system (DCS) of thermal power plant, the NOx concentration fluctuates drastically during the blowback, so it is easy to obtain abnormal values of the NOx concentration, which cannot be used for analysis. In fact, the NOx concentration is usually correlated with O2 content, the reason being that the measured NOx concentration is corrected by the standard O2 content. In addition, most significant factors affect the inlet NOx concentration in the literature [5], and the O2 content has the greatest influence on the inlet NOx concentration. Based on the above factors, this paper proposes estimating the lag time by using the purge signal of the CEMS and the variation of inlet O2 content, and then the lag of the inlet NOx concentration is obtained.
Figure 2 shows that the inlet NOx concentration during the blowback fluctuates drastically because air is used during the blowback. So, the maximum O2 content is 21%, and the change time for the inlet NOx concentration and inlet O2 content are the same as the blowback time, i.e., 3 min. So, it shows that it is more convenient and accurate to use the inlet O2 content to estimate the lag time of the NOx analyzer.
Figure 3 shows that when the blowback signal is 1, the blowback starts, and the lag time can be judged by the rise time of inlet O2 content at the moment of the blowback. Similarly, when the blowback signal is 0, the blowback has ended, and the CEMS will re-pump the flue gas, and the lag time can also be estimated by the fall time of the inlet O2 content. In addition, Figure 3 shows that the rise time and fall time of inlet O2 content are basically the same, and the lag time can be determined at 60 s.

3. Data-Driven Model of the Inlet NOx Concentration

To implement the data-driven model of the inlet NOx concentration, it is necessary to first analyze the main influencing factors of the inlet NOx concentration and determine the input variables of the inlet NOx concentration prediction model. In addition, data pre-processing should be carried out, which includes dynamic correction of abnormal data points, online filtering and pre-processing of the blowback process.

3.1. Input Variables

The inlet NOx concentration is mainly related to the boiler combustion process, and the main factors of the process are obtained by analyzing the relevant factors of the boiler combustion process. According to the analysis of thermal NOx and fuel-based NOx generation process, NOx generation is mainly influenced by the following factors. In addition, the combustion zone temperature and O2 content are both related to NOx generation.
(1) When the power plant is put into automatic gain control (AGC), the load will fluctuate continuously, which will directly affect the total coal feed rate and total air volume. Since the total coal feed rate and total air volume changes are not synchronized, the air–coal ratio changes, thus affecting the variation of O2 content and leading to the fluctuation of the inlet NOx concentration.
(2) When the opening of combustion air baffle changes, it will also lead to unbalanced air combustion classification, and it will cause changes for the temperature field and O2 content distribution in the combustion area, which in turn leads to the variations of the inlet NOx concentration.
(3) The start and stop of the coal mill also affect the boiler combustion process, and causes the air–coal ratio to change, thus causing the O2 content in the boiler to change, which in turn causes the inlet NOx concentration to fluctuate.
According to the field data, the input variable data for the inlet NOx concentration data-driven model were determined as shown in Table 2. Since the data from the boiler are obtained earlier than the data from the SCR system, the model can be built by the variable data from the boiler side to predict the inlet NOx concentration in advance.

3.2. Data Pre-Processing of Blowback Process

This paper adopts the method of linear interpolation to preprocess the inlet NOx concentration signal for the CEMS blowback process, because the signal of the CEMS blowdown has periodicity. According to the analysis of field data, the CEMS will execute a continuous 3 min blowback at about 4 h intervals. Because there are still some abnormal data points after the end of blowback process, the data preprocessing needs to increase the data of the blowback time. In this paper, the data of the inlet NOx concentration is measured for a period of 1 s. For example, data preprocessing uses 280 data every 14,300 data by Equation (1).
x ^ t = x 1 + x m x 1 m t 1 ,   1 < t m
Here, x ^ t is the inlet NOx concentration at time t after preprocessing, m is the number of purge data processing points, x 1 is the inlet NOx concentration at the start of blowback process, and x m is the inlet NOx concentration at the end of blowback process. The pre-processed results of the inlet NOx concentration during the CEMS blowback process are shown in Figure 4. It can be seen from Figure 4 that all abnormal data points during the blowback process are eliminated.

3.3. Data-Driven Model of the Inlet NOx Concentration

The data-driven model of the inlet NOx concentration in many studies [1,2,3,4,5,6,7,8,9,10] is mainly one which only predicts the inlet NOx concentration in advance for the current time and uses times series data to validate the model. There are two main drawbacks. One is that the predicted values are affected by the mean and standard deviation of the training set. So, it is impossible to track the curve changes in time when the inlet NOx concentration fluctuates drastically. The other one is that the model parameter search is generally computationally time consuming. So, it is impossible to predict the inlet NOx concentration in multiple steps in advance, which is contradictory to the purpose of the inlet NOx concentration for a feedforward signal.
The exponential prediction can predict the inlet NOx concentration, which can predict the true value in advance for a longer period of time [22]. In order to compensate for the output bias of the exponential prediction model, this paper proposes an improved exponential prediction model. The schematic diagram is shown in Figure 5.
First, the predicted inlet NOx concentration at time t is obtained based on the exponential prediction model at time t-L, and then, the deviation between the predicted value and the measured inlet NOx concentration at time t is obtained. The deviation prediction model is established by RLSSVM. The model predicts the future L-step deviations between the values of the exponential prediction model output and the real values of the inlet NOx concentration, as shown in Equation (2). The output value of the RLSSVM model adds the output value of the exponential prediction model to achieve the purpose of correcting the exponential prediction model output.
Δ y ^ t + L = F x t = f Δ y ^ t , u t , u t 1
Here, u represents the input variable of the exponential prediction model. Δ y ^ t represents the deviation between the real value of the inlet NOx concentration at step t and the predicted inlet NOx concentration by the exponential prediction model.

3.3.1. Exponential Prediction Model

According to Table 1, the input variables of improved exponential model were determined. A numerical model established the exponential prediction model of the inlet NOx concentration. The equation is as follows.
y NO = A × [ ( B W 1 ) a C ] × [ ln ( W 2 ) β ] [ D ( W 3 ) γ ] × [ ( W 4 ) δ E ] × [ ( W 5 F ) ε G ]
Here, W1 is the total air volume, W2 is the average opening of secondary air register, W3 is the boiler load, W4 is the air–coal ratio, and W5 is the O2 content of flue gas in the boiler outlet. Each of the above parameters is determined by non-linear fitting experiments, and the parameters are adjusted according to the operational condition of the boiler and the SCR system.

3.3.2. Recursive LSSVM (RLSSVM) Model

(1)
LSSVM Model
Suykens et al. [23] proposes LSSVM by improving the quadratic optimization problem of SVM. LSSVM uses the least squares method to transform the SVM learning into solving the problem of linear equation. So LSSVM reduces the computational complexity and has a better prediction accuracy.
Let the training set W = { x i , y i x i R n , i = 1 , 2 , , n } , x i is the input sample point, and y i is the output sample point corresponding to x i , then the SVM problem is represented by a simple transformation as
min J ω , e = 1 2 ω T ω + C 2 i = 1 l e i 2
s . t . y i = ω T ϕ x i + b + e i ,   i = 1 , 2 , , n
A Lagrangian function is established to turn the constrained optimization formula into an unconstrained optimization formula.
L ω , b , e ; a = 1 2 ω T ω + C 2 i = 1 l e i 2 + i = 1 n a i y i ω T ϕ x i b e i
The KKT condition, then, is
L ω = 0 ω = i = 1 n α i ϕ x i L b = 0 i = 1 n a i = 0 L e i = 0 a i = C e i L α = 0 ω T ϕ x i + b + e i y i = 0
After eliminating e i and ω , Equation (7) can be rewritten as
0 I T I K b α = 0 y
Here,
I = 1 1 , 1 2 , , 1 n ] T ,   α = α 1 , , α n ] T ,   y = [ y 1 , , y n ] T
δ i j = 1 ,   i = j i ,   j = 1 , 2 , , n 0 ,   i j
According to Equation (10), it can be seen that the training problem of LSSVM boils down to a solution problem of linear equations, so the training speed of LSSVM is faster than the training speed of SVM. The solution for α and b are as follows.
b = I T K 1 y I T K 1 I
α = Κ 1 y I I T K 1 y I T K 1 I
The LSSVM model is obtained as Equation (13). The kernel function uses the radial basis function.
y ^ x = i = 1 n α i k x , x i + b
(2)
RLSSVM Model
Assume the kernel matrix at time t is as follows [24].
Q t = k x 1 , x 1 k x t , x 1 k x 1 , x t k x t , x t
K t = Q t i , j + δ i j C = ϕ ( x i ) T ϕ x j + δ i j C , so
K t = k x 1 , x 1 + 1 C k x t , x 1 k x 1 , x t k x t , x t + 1 C
At time t + 1, a new sample x t + 1 , y t + 1 is obtained. Similarly
K t + 1 = k x 1 , x 1 + 1 C k x t , x 1 k x t + 1 , x 1 k x 1 , x t k x t , x t + 1 C k x t , x t k x 1 , x t + 1 k x t , x t + 1 k x t , x t + 1 + 1 C
At time t + 1, K t + 1 can be written as a block matrix as follows
K t + 1 = K t     V t + 1 V ( t + 1 ) T     v t + 1
Here, V t + 1 = [ k x 1 , x t + 1 , , k x t , x t + 1 ] T ,   v t + 1 = k x t + 1 , x t + 1 + 1 C .
Equations (11) and (12) involve the inverse of kernel matrix, so
K ( t + 1 ) 1 = K t V t + 1 V ( t + 1 ) T V t + 1 1 = K t ] 1 0 0 0 + r t + 1 r ( t + 1 ) T z t + 1
Here, r t + 1 = ( V ( t + 1 ) T K ( t ) 1 , 1 ) T , z t + 1 = 1 v t + 1 V ( t + 1 ) T K ( t ) 1 V t + 1 .
Equation (18) shows that the K t + 1 can be obtained recursively from the K t at the previous moment and the newly added sample v t + 1 .

3.4. Simulation Experiment

The prediction model of the inlet NOx concentration is developed. The simulation data come from field data from an operation condition near 800 MW. The parameters of the exponential prediction model were finally determined by optimization algorithm, as showed in Table 3. For the exponential prediction model, the comparison of the predicted values and real values are shown in Figure 6.
Figure 6 shows that from point 500 to point 1300, the boiler is in steady-state operation condition. So, the predicted values from the exponential prediction model are relatively well fitted with the real values, and the root mean square error (RMSE) value is 6.8990 mg/m3. However, from point 200 to 300, the inlet NOx concentration increases as increased total air volume, and the lag time of the NOx analyzer can be estimated at 100 s or so based on the time difference between the rising curves of the predicted and real values. From point 1300, the predicted values and real values of the inlet NOx concentration show a large deviation due to the increase in load from 800 MW to 900 MW. The predicted value is higher than the real value, and the RMSE value is 26.7963 mg/m3. In all, the exponential prediction model can track the curve change when the inlet NOx concentration changes significantly, but the disadvantage is that the predicted values from the exponential prediction model have some deviation from the real values when the boiler is exposed to variable operational working conditions. If the prediction value of the exponential prediction model under variable operating conditions is higher than the real value, it is easy to cause the SCR system to over-regulate the amount of NH3 injection and cause NH3 slip, so the amount of feedforward control usually adopts the speed limit and amplitude limit measures. On the one hand, the time delay of the model can be set at 60 s. On the other hand, the RLSSVM is used to predict the output deviation of the exponential prediction model and correct the output deviation. Taking the 600th to 1800th points of the inlet NOx concentration as an example, the prediction curves of output deviation of exponential prediction model are shown in Figure 7.
According to Figure 7, the exponential prediction model output deviation can be predicted 60 s in advance with a high prediction accuracy by using the improved exponential prediction model, which indicates that the deviation value is corrected in real time by using the RLSSVM model, and the trend change in the deviation prediction curve is basically consistent with the real value. Then, the relative errors and the comparative results between the improved exponential prediction model and exponential prediction model are shown in Figure 8.
Figure 8 shows that the relative errors of two models are small before the 1300th point, when the boiler is under steady-state conditions. From the 1300th point, the relative errors of the two prediction models increase, but the relative errors of the improved exponential prediction model are smaller compared with the exponential prediction model. The experiment results show that the improved exponential prediction model can make the predicted values of the inlet NOx concentration under variable working conditions closer to the real values of the inlet NOx concentration, thus effectively avoiding the problem of high predicted value when using an exponential prediction model and, to a certain extent, avoiding the phenomenon of excessive NH3 injection when using the exponential prediction model output as the feedforward signal.

4. Improved Feedforward Control Based on the Data-Driven Model of the Inlet NOx Concentration

For a NH3 injection control system, the inlet NOx content is obtained by multiplying the inlet flue gas flow and the inlet NOx concentration, and it is often introduced in the control logic as a feedforward signal to achieve feedforward control [25]. In order to quickly respond to the condition changes on the perturbation of the inlet NOx concentration under different operation conditions, the lag time of the SCR reaction and flue gas analysis can be compensated to a certain extent. However, the feedforward control method is not ideal because of the response lag of the NOx analyzer in the SCR system. So, this section achieves the goal of improving the feedforward control by predicting the inlet NOx concentration in advance and using it as a feedforward signal.

4.1. Control System Structure

To further improve the PID control effect, the improved exponential prediction model output of the inlet NOx concentration is used as a feedforward signal to improve feedforward control. The block diagram of an NH3 injection composite control system based on an improved feedforward control and PID control is detailed in Figure 9.
In Figure 9, the real-time predicted value of the improved exponential prediction model output is used as the feedforward signal, and the NH3 injection valve opening variation Δ n N H 3 is used as the feedforward control parameter. Δ n N H 3 is converted from the improved exponential prediction model output by the following equation.
Δ y N H 3 = Δ C N O x × Q × M N H 3 × η N O x M N O x × 10 6
Δ n N H 3 = Δ y N H 3 k
Here, Δ C N O x is the change in the inlet NOx concentration after improving feedforward control, mg/m3. That is the difference between the improved exponential prediction model output and the measured inlet NOx concentration at the current moment t. Q is the inlet flue gas flow rate, m3/h. M N H 3 and M N O x are the molar masses of NH3 and NOx. η N O x is the SCR de-NOx efficiency, %. Δ y N H 3 is the variation of NH3 injection flow after adding feedforward control, kg/h. k is the linear coefficient between the variation of NH3 injection flow and the variation of NH3 injection valve opening. In general, NH3 supply pressure remains unchanged, so the intermediate distance between the NH3 injection valve opening and closing is a linear relationship. In this paper, according to the samples of the NH3 injection flow and NH3 injection valve opening, k = 3.82744.
The feedforward signal of the inlet NOx concentration can be predicted 60 s in advance and then through the feedforward control, so the PID controller can realize the early action of NH3 injection valve to control the amount of NH3 injection and adapt to the change in operation conditions.

4.2. Simulation Experiment

Before studying the control strategy for NH3 injection, this section analyzes the effect of the inlet NOx concentration measurement lag on the control system and the analysis of the control effect with the improved feedforward control.
First, the lag of the inlet NOx analyzer on the control system is analyzed, and then the absolute error between the measured values and the real values of inlet NOx are analyzed based on the lag time determined in Section 2.2, as shown in Figure 10.
Figure 10 shows that there are deviations between the measured and real inlet NOx to the influence of lag. The deviations are much bigger when the inlet NOx concentration fluctuates drastically. The absolute error reaches up to 73 mg/m3. Therefore, in order to ensure the effect of the NH3 injection control, the lag influence of the inlet NOx analyzer on the control system must be considered.
The control effect of the composite control based on the improved feedforward (IF) control and PID control (IF-PID), and the PID control is compared with: the IF-PID control on the outlet NOx concentration, as shown in Figure 11; the NH3 injection flow rate, as shown in Figure 12; and the optimization index, as shown in Table 4.
According to Figure 11, the measured values of the inlet NOx concentration deviate significantly from the real values of the inlet NOx concentration. It can be seen that the improved feedforward control can make the NH3 injection valve operate earlier at the peaks and troughs of the outlet NOx curve. Compared with the feedforward control, the outlet NOx concentration converges to the set value of 37 mg/m3. It indicates that the HP-PID control can reduce the excessive NH3 injection and the NH3 slip to a certain extent. On the one hand, the cost of NH3 injection is reduced, and sustainable development of the enterprise is achieved; on the other hand, NH3 slip is reduced, so air pollution is avoided, and environmental sustainability is achieved.
According to the optimization index results in Table 4, the average outlet NOx concentration is slightly reduced, the standard deviation of the outlet NOx concentration decreases 20% (most outlet NOx concentration points meet the national environmental protection regulation), the average de-NOx efficiency remains the same, and the average NH3 injection flowrate and average NH3 slip are slightly reduced. It indicates that the inlet NOx data-driven model based on the exponential prediction model and the RLSSVM can accurately predict the inlet NOx concentration in advance, and the NH3 injection control effect can be improved by improving the feedforward control.
Figure 12 shows that the IF-PID control further increases the NH3 injection flow rate from point 1300 to point 1500 compared with the PID control, which reduces the outlet NOx concentration but exceeds the maximum value of the NH3 injection flow rate when the PID control is used. According to the analysis of the field data, the NH3 injection valve opening reaches 50% at the 1300th to 1500th points using PID control, indicating that the actuator of the NH3 injection valve has reached saturation at this time when an automatic control is used. Therefore, the outlet NOx concentration is too high through the IF-PID control. The amount of NH3 injection appears to overshoot. In field, if the actuator saturates during automatic control, the control effect will be adversely affected.
In addition, the feedforward control can make the NH3 injection valve act in advance according to the change in the inlet NOx concentration data-driven model. However, to some extent, the response lag of the PID control is due to the lag in the feedback signal of the outlet NOx concentration. Because the CEMS is installed at the outlet of the SCR reactor, the measurement lag of outlet NOx should not be neglected.

5. Conclusions

The output of the inlet NOx concentration data-driven model is used as a feedforward signal, which can improve the feedforward control. The IF-PID control has a compensating effect when the boiler is under variable operation conditions, and the adaptability of the SCR system to variable operation conditions is improved. By improving the feedforward control, the NH3 injection valve can be operated earlier, which enhances the timeliness of the system in variable operation conditions. The validity of the model is verified in this paper. Furthermore, the better effect of NH3 injection control and environmental sustainability are achieved without increasing the cost of NH3 injection.
In future research, in order to further improve the control effect, model predictive control can be considered instead of PID control to achieve rapid feedback of the outlet NOx concentration signal.

Author Contributions

C.L.: conceptualization, methodology, validation, writing. B.H.: methodology, writing. Y.Y. and M.S.: validation. G.X.: validation, writing. L.Q.: conceptualization, methodology. Z.D. and L.Y.: conceptualization, validation. All authors have read and agreed to the published version of the manuscript.

Funding

This research was funded by the Hebei Provincial Science and Technology Program (S&T Program of Hebei, Project No. 22567643H).

Conflicts of Interest

The authors declare no conflict of interest.

References

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Figure 1. Schematic diagram of CEMS at the inlet of SCR de-NOx system.
Figure 1. Schematic diagram of CEMS at the inlet of SCR de-NOx system.
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Figure 2. Inlet NOx concentration and inlet O2 content at the time of blowback.
Figure 2. Inlet NOx concentration and inlet O2 content at the time of blowback.
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Figure 3. Analysis of the lag time.
Figure 3. Analysis of the lag time.
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Figure 4. Data preprocessing of inlet NOx concentration in the blowback process of CEMS.
Figure 4. Data preprocessing of inlet NOx concentration in the blowback process of CEMS.
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Figure 5. Schematic diagram of improved exponential prediction model.
Figure 5. Schematic diagram of improved exponential prediction model.
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Figure 6. Comparison of predicted values and real values of inlet NOx concentration.
Figure 6. Comparison of predicted values and real values of inlet NOx concentration.
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Figure 7. Prediction curve of output deviation of the exponential prediction model.
Figure 7. Prediction curve of output deviation of the exponential prediction model.
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Figure 8. Comparison of the relative errors of the predicted values between the improved exponential prediction model and the exponential prediction model.
Figure 8. Comparison of the relative errors of the predicted values between the improved exponential prediction model and the exponential prediction model.
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Figure 9. Block diagram of NH3 injection composite control based on improved feedforward control and PID control.
Figure 9. Block diagram of NH3 injection composite control based on improved feedforward control and PID control.
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Figure 10. Absolute error between the measured values and the real values of inlet NOx concentration.
Figure 10. Absolute error between the measured values and the real values of inlet NOx concentration.
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Figure 11. Outlet NOx concentration of IF-PID control and PID control.
Figure 11. Outlet NOx concentration of IF-PID control and PID control.
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Figure 12. NH3 injection flowrate of IF-PID control and PID control.
Figure 12. NH3 injection flowrate of IF-PID control and PID control.
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Table 1. Different data-driven techniques in the literature.
Table 1. Different data-driven techniques in the literature.
LiteratureData-Driven
Model
Dynamic ModelModel SimplificationDelay
Estimation
Prediction
Period
Shakil et al. [6]NNYesYesYes Current
Hsieh et al. [7]Kalman
filtering
//Yes Current
Peng et al. [8]SVR/Yes/ Current
Lv et al. [9] LSSVM /Yes/ Current
Li et al. [10] MWPLS Yes Yes/ Current
Ahmed et al. [11] LSSVM Yes //Long-term
Yang et al. [12] LSSVM Yes /YesLong-term
Xie et al. [13] LSTM Yes /YesLong-term
Matsumura et al. [14] LSSVM //YesLong-term
Kříž et al. [15]Chaos Theory//YesLong-term
Kang et al. [16] biLSTM //YesLong-term
Song et al. [17] LSTM ///Long-term
Liu et al. [18] LR ///Long-term
Wu et al. [19] LSTM /Yes/Long-term
Yuan et al. [20] SGEM /Yes/Long-term
Li et al. [21] Improved model ///Long-term
This paper Improved
model
YesYesYes/
quantitative
Long-term
Table 2. Input variable data of inlet NOx concentration data-driven model.
Table 2. Input variable data of inlet NOx concentration data-driven model.
Main influencing FactorRelated ParametersParameter Range
Boiler loadBoiler load677 MW~896 MW
Burning coalWind–coal ratio0.876~1.0793
Combustion conditionOutlet O2 content2.76~4.25%
Total air volume2787 t/h~3601 t/h
Excess air coefficientAverage opening of secondary air damper42.16~48.75%
Table 3. Parameters of inlet NOx concentration exponential prediction model.
Table 3. Parameters of inlet NOx concentration exponential prediction model.
A/(mg/m3)BCDEFGαβγδ
1250.80.010.520.50.1550.050.8
Table 4. Optimization index of IF-PID control and PID control.
Table 4. Optimization index of IF-PID control and PID control.
IndexIF-PIDPID
Average de-NOx efficiency/(%)80.091880.0001
Average NH3 slip/(ppm)1.75171.7358
Average NH3 injection flowrate/(kg/h)69.844569.6047
Average outlet NOx concentration/(mg/m3)37.229537.1478
Standard deviation of outlet NOx concentration/(mg/m3)5.84914.6684
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Liu, C.; Hu, B.; Song, M.; Yang, Y.; Xian, G.; Qu, L.; Dong, Z.; Yan, L. Prediction and Control of the Nitrogen Oxides Emission for Environmental Protection Goal Based on Data-Driven Model in the SCR de-NOx System. Sustainability 2022, 14, 12534. https://doi.org/10.3390/su141912534

AMA Style

Liu C, Hu B, Song M, Yang Y, Xian G, Qu L, Dong Z, Yan L. Prediction and Control of the Nitrogen Oxides Emission for Environmental Protection Goal Based on Data-Driven Model in the SCR de-NOx System. Sustainability. 2022; 14(19):12534. https://doi.org/10.3390/su141912534

Chicago/Turabian Style

Liu, Chang, Bo Hu, Meiyan Song, Yuan Yang, Guangquan Xian, Liang Qu, Ze Dong, and Laiqing Yan. 2022. "Prediction and Control of the Nitrogen Oxides Emission for Environmental Protection Goal Based on Data-Driven Model in the SCR de-NOx System" Sustainability 14, no. 19: 12534. https://doi.org/10.3390/su141912534

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